S3 Thunderbolt Converting from EFI to CarburetorThe advent of electronics has brought about many changes in all industries across the board with greater and more precise control however, to some of us not all of these changes are for the better. I know that electronic control is about the only way vehicles are going to meet the government’s expectations of pollution control, the people’s expectations of greater miles per the ever expensive gallon of fuel, and in the right hands a riders expectations of unreal performance. But for some of us the electronic control ain’t always the way to go. I thought it was a good idea when the electronic ignition first came along and I no longer had to deal with setting points (I can still set them but I’m lazy). In the simpler form there weren’t the myriad of peripheral sensors and multitude of settings, just a black box and cam position sensor and that suited me just fine. Personal opinion out of the way there are some communist states in America that will get bent out of shape if you convert from EFI to carbureted so you better check before you proceed. If you happen to live in one of those states then I truly feel for you for your options are few; Be happy with what you’ve got and learn to live with it, Get an older machine, or MOVE. But for the rest of us who ain’t electronic geeks, have a thing for the carby, and live in one of the few remaining free states then greetings brothers and sisters.
I must apologize for the lack of disassembly pictures but Mike got a bit over zealous and started the tear down before I got there so I’ll do the best I can to keep you in step. First the negative cable
from
the battery was disconnected then the positive then the battery was
removed. The seat, air cleaner stuff and the rear fairing was removed.
Then on to the fuel tank, NOTE:
make We are replacing the 2 X 12 pin Electronic Control Module with an 8-pin ignition module with the idea of upgrading to the Crane HI-4E later (also an 8 pin). I spent a few hours going over the manuals and the different wiring diagrams mapping out the wiring using the Deutsch DT connectors that come stock. I like these connectors for the environmental resistance and ease of disassembly. The Deutsch website has excellent references on installation. There are a few issues with the conversion:
First is the butt load of ECM controlled sensors with the DDFI and the loss of the electronic engine analysis the ECM provides. Second is the electronic speedometer (the 8 pin is set up for a mechanical). Third is the jumping of the tachometer and coil (the Delphi controls both separately through the ECM). Forth the ignition/starter relay block has some changes. Finally is the addition of the Vacuum Operated Electronic Switch (V.O.E.S.). The sensors have one of two ways to be dealt with: disconnect and remove the sensor then cap off the terminals leaving the harness wiring intact (easy way) or (since I was doing surgery anyway) remove the sensor, connector and associated wiring up to any splice. I removed the braiding from the wiring harness from the dash connectors to the battery box. The harness that went behind the battery box and toward the swingarm was left intact and the wires to the unused sensors were clipped as close as possible to the wrapping. I also removed the braiding from the Ignition/Starter Relay Block to the part where the forward braiding was removed. The tape was then removed from the harness where the braiding was removed. It looked like the bike was hemorrhaging wires. All splices that were made are soldered and shrink tube was used over the splice to make them weather/fuel resistant. The Violet/Yellow wire from the Throttle Position Sensor is used to replace the Violet/White lead that would normally be used for the V.O.E.S. We kept the O2 sensor on the exhaust manifold for now and will replace it later for the input on a K&N air/fuel ratio monitor. The Speed Sensor (easy to spot it has three heavy wires twisted together from the front all the way down to the tail) was retained since we kept the electronic speedometer instead of swapping out a mechanical one. The clock was removed, as the K&N fuel/air monitor will occupy the space in the dash.
To have a working tachometer the pink lead from the tachometer was clipped and spliced into the Blue/Orange lead for the coil. The Ignition/Starter
Relay Block was
next. First the
White/Black lead was pulled from the block and the female spade
connector was
clipped. The insulator was trimmed back and a male Deutsch DT pin was
crimped
on. This was inserted into pin position 1 of a male Deutsch DT 8-pin
connector
for the Ignition Module and checked against the new ignition module
connector
for proper routing. That was the easy part. I clipped the Gray/Orange
lead that
goes to the ignition power switch leaving about 5” of wire connected to
the
block. CAUTION;
make sure it is the one going to the ignition
switch and NOT
the one going to the fuse block). I trimmed back the
insulation and crimped
on a 3/16” female spade connector. I could not find the connector that
is made
to fit this style block locally so I removed the plastic collar from a
common
3/16” female spade and with a pin punch pushed out the center slightly
to grab
the block as the replacement would. This connector is then inserted
into the
Ignition/Starter Relay Block where the White/Black lead connector was
pulled.
The other clipped end of the Gray/Orange ignition power switch lead is
then
spliced into the power (Gray) wire.
Now we moved on to the meat: the ignition module. The Electronic Control Module is unplugged and removed from the chassis and replaced by the 8-pin ignition module. Both of the Deutsch DT 12-pin connectors (Gray and Black) are pulled apart. The pins were removed with the wires of the unused sensor connectors and the sensor wiring was set aside. The female pins for the Cam Position Sensor (Red/White, Black/White, and Green/White) were removed and replaced by males and then
A 2-pin male Deutsch DT
connector was
then used for the
V.O.E.S. a second male pin was connected to the free end of the
Violet/Yellow
wire and I re-checked all connections for integrity and placement re-enforced sleeves were then added to the new connector installs. The wiring harness was then bundled with electrical tape then split plastic conduit was added and then the harness was secured against the frame. I made sure that the wiring was away from hot or moving engine components as well as not interfering
I pulled the DDFI tank out and started to drain the old fuel in a gas can when I noticed gelling had taken place. The gas had sat too long in the tank and de-stabilized resulting in translucent snot looking globs floating in the old gas. I chucked the old fuel (about 1/2 gal into our waste chemical drum and thoroughly cleaned out the tank. I removed the inlet ring, vent and rubber then removed the fuel pump. We ran into a re-occurring issue with the Buell body parts. With the exception of the engine, frame, swingarm and a few brackets the Buell is largely plastic. Plastic has allot of fine qualities; it is lighter than metal, it has a better memory than
When bonding or sealing agents are used strength of bond and fluid resistance are the primary concern. Now that you have insight into my brain I show you my solution to the problem of securing the Pingel Petcock to the plastic DDFI Buell tank. After the tank was gutted and cleaned I assessed the situation; two holes in the tank about 4" apart, one has to be sealed off and the other has to accept the 7/8 UNF 14 thread of the Pingle DDFI to petcock adapter. The only adapter Pingle makes for DDFI to Carby is for the Harley-Davidson Delphi System with metal fuel tanks and not the Buell Dephi system for the plastic tanks. Apparently the Buell system has a small thread size so I could not use the thin nut or rubberized washers from the old fuel pump (as I anticipated). First I tried to get a 7/8 UNF 14 nut in stainless but no go the local dealer only had it in steel. I took the 7/8 nut to the grinding bench
The surfaces of the tank that was to get the bonding agient (JB WELD) were thoroughly cleaned and scuffed to roughen the surface. The nut had bond applied then installed through the inside of the tank, then the plate had bond applied and set in place. The adapter had teflon tape wrapped on threads and screwed into the nut then torqued down. The whole works was set up to cure overnight. While Mark and I were searching for parts in the shop we ran across the Thunderbolt's front shroud. I thought the X1 add on was a style choice of Marks but it turns out the S3 was laid down resulting in damage to the shroud and instead of fixing it Mark went with plan B. He said he would like it fixed and reinstalled so while I was waiting on parts I decided to press on to body work. The right turn signal and mirror were history but the shroud only had a small crack at the base of the mirror on the left hand side. I used JB weld and some window screen mesh as backing on the crack, after it cured only a small white scar was visible.
When I remounted the headlight assembly I noticed that the most of the adjusting screws and clips were missing. This meant a floppy headlight in the cradle so more parts to order. Under the old parts manual the entire headlight assembly has to be ordered (which is costly) under the new parts numbers the clips and adjusting screws can be ordered separately (at much less cost). When I re-mounted the shroud I noticed that the top spreader bar on the shroud frame was bent in slightly (1-1/2") so I bent it back out with some low heat and a pry bar. I snapped on the shroud and another small victory celebration ensued. |